Pistons are in – part 2

While I was tightening conrod bolts, I found out that the bolt head was not 10mm.

Totally forgot that ARP does not come from metric world. Almost shat my pants when I felt the tool slip – luckily it was just the socket giving up.

Figured out pretty quickly that the bolt head must be 3/8″, which converts neatly to 9.5mm, and just to make sure that the size wasnt something really weird I also bought a 9mm socket.

Perfect fit – it was 3/8″. I cleaned everything twice and tightened the bolts to 40Nm per instructions from conrod manufacturer.

Heading towards this:

Meanwhile Widric had bought a disco ball.

Pistons are in

After quickly checking the shop manual that I wasnt forgetting anything (like those ring pins), I rummaged through Widrics stash for a piston ring compressor.

Quick check from the internet how the piston ring gaps should align and in they went.

All four went in nicely, no hiccups, very smooth movement and no obivious problems.

From below, bolts are in place but not yet torqued.

After getting back home, a cold surprise from Hokkaido!

Crank and block part 2

I got some comments recently from bot, who suspected that the middle main cap deforming while ARP nuts were tightened could be the reason behind my seized crank.

The possibility of twisted or tweaked middle main cap didnt cross my mind. I had already gotten my block back from machine shop, when bot commented this thing, but I didnt have spare time to actually look my block until now.

I spent two hours carefully taking everything apart and examining the parts (once again). Block still had some cutting oil + metal particle residue from the honing and it probably was also mixed with that ARP moly stuff that was used on the threads. It took some time to get everything clean.

Below: I made a set of cylinder plugs from foam plastic to help with cleaning and installing parts.

Putting everything back together went well. Bearings and ARP studs went in smoothly and so did the crank (after cleaning it millionth time). When I got to the thrust bearings I eyeballed them with suspicion but they didnt reveal anything to me. Lower ones slid in easily and the upper ones went in with the main cap.

Last bits were the MRP girdle and ARP washers and nuts. I tightened the nuts in four steps starting from 20Nm and ending to 80Nm, stopping in between to rotate the crank and see if there were any problems. The crank rotated freely every time.

Below is my torque wrench. I bought this one just for this project to get the critical parts correctly torqued.

It started to seem that the honing did help and the middle cap wasnt causing any trouble. I grabbed the crank from the both ends and tried to shake it, but it felt like there wasnt any play. I went to get Widrics almost unused dial indicator and set it up.

Below: zeroed

Then I poked the crank with screwdriver like the Toyota manual says.

Result: seems that my crankshaft end play is 0.03mm. Toyota manual says that the minimum acceptable is 0.02mm 😀

Some thoughts:

I’ve introduced plenty of new parts to my engine block. I have new main bearings and new thrust bearings, both with extra moly coating on them. Also, a set of longer ARP studs (with washers and nuts) for the girdle and the girdle itself.

Every new part creates a huge number of unknowns and it is absolutely important to check that everything is where they should be. Mr. Manon probably disagrees with me, but even the girdle could have been the source for my problems, although it got complemented by the machinist doing the honing 😀

Just by fitting all the parts together I found out that the middle main cap was not the problem. I’m not entirely happy of this method, but it has to do now. I dont have the resources and possibilities of McLaren to build engines 😀

Edit: My preferred method for the problem would have been different. I prefer to measure things until I have numbers, results and hard evidence. Except putting things back together was more practical and efficient method… 😀

I didnt measure the bearings yet, so next time I’ll be messing with plastigage.

and _o/ to bot!

The tide has turned part 2

After the crank got stuck, I disassembled everything:

Bearings looked still good and the molybdenium coating was not affected.

Little bit of measuring – picture below is staged 😀

While having the girdle plate on and everything tightened, the crank bore shrunk to 51,98mm. Didnt expect to see chunks of steel deform so much that the crank line bore would be out of spec (it should be 52mm)

Well, this meant a trip to machinist. Assembled everything back and made sure that the block and girdle were ready for the crank line honing.

Before honing:

…and after honing:

Plenty of cleaning ahead, but the machinist said that the inside diameter  is now 52.03mm.

The crank was also checked for straightness. Weirdly enough, it was 0.03mm out of straight, but now only 0.02mm. For some reason being stored for a year made it little bit more straight 😀


The tide has turned part 1

I reached the turnaround point! Now I’m putting things back together and going towards working engine 🙂

There were problems, though.

New ACL bearings coated in solid molybdenium for extra slippery and first start safety.

Crank test fit. Stock bolts and oil pump.

Rear main seal bracket and the seal itself. Below, the gasket for the bracket.

Seal in place. Left side you can see the 22221 number which indicates the crank line bore sizes.

Glueing the crank girdle to place with Permatex Supra Grey. Main bolts swapped to ARP studs and nuts.

This is where the problems started.

I left the gasket goop to dry for an hour and came back to tighten the main stud nuts. I quickly glanced the ARP installation procedure and thought that it is funny how ARP recommends the tightening torque to be the same as Toyota stock, which is 60Nm. Tightened everything in three steps and then I tried to rotate the crank. It wasnt turning as freely as I hoped.

I checked everything. Removed nuts, removed studs and checked everything possible. Tried tightening again to 60Nm but no dice. There still was a point where the crank felt like it was stuck. Then I read the ARP installation document again and to my horror ARP recommendation wasnt 60Nm, instead it was 60ft/lbs, which is around 80Nm.

The crank seized totally. It only turned a bit when I helped it with the biggest rubber mallet I could find in our garage. Shit shit shit fuuuuuck.

Buttloads of stuff

Lots of stuff coming in!

The cutest package from Thailand:

Cute box contained connectors for Toyota coil on plugs. Most likely fake as fuck but hopefully they work enough.

Pistons, again.

Arp hardware – studs and bolts. No cat this time.

Engine management unit from MaxxECU, with long loom, lambda sensor and stickers!

The turbo – BorgWarner EFR 6258. Hardware kit needed.

Toyota coil on plugs (dirty and used) – look how the last one is bit short and stubby compared to the rest of the coils. The last one is from Yaris and the long and skinny ones are from Lexus. Funny thing is that I ordered four Yaris ones but got three Lexus coils and one Yaris.

Not going to complain, because the Lexus coils seem to fit pretty well into 4A head. 🙂

Lexus coil part number – 90919-02246